Since I rebuilt the engine, my '79 (Pamco, stock advance, stock carbs, stock airboxes and elements) has been backfiring badly on deceleration, particularly on the right side.
When I rebuilt the engine I ran the carbs through a sonic cleaner and installed carb kits from Mikes (yeah, I know...) and recently put in new Genuine Mikuni floats as the left one sprung a leak. Float level is right on.
I've double checked the valve gap (all good, right exhaust was just a tad loose) and the cam chain tension, synched the carbs by checking for equal exhaust pressure, and backed the idle mixture screws out to 3 turns.
Starts good, idles good, plugs look good, just backfires a LOT on deceleration.
Gonna resynch the carbs with my home made manometer, but I'm relatively confident they're pretty close.
So, I guess my question is, What Next?
Should I scrap the Mikes jets and go back to the stockers? I didn't have a real reason to change, I did it "just because". AFAIK, they were the same jet sizes, but I didn't write it down so that could be part of the problem I guess.
Looking at three days of heavy rain so this is the perfect time to putter in the garage for a while. Got to put my new clutch and throttle cables from 650 Central on anyway.
When I rebuilt the engine I ran the carbs through a sonic cleaner and installed carb kits from Mikes (yeah, I know...) and recently put in new Genuine Mikuni floats as the left one sprung a leak. Float level is right on.
I've double checked the valve gap (all good, right exhaust was just a tad loose) and the cam chain tension, synched the carbs by checking for equal exhaust pressure, and backed the idle mixture screws out to 3 turns.
Starts good, idles good, plugs look good, just backfires a LOT on deceleration.
Gonna resynch the carbs with my home made manometer, but I'm relatively confident they're pretty close.
So, I guess my question is, What Next?
Should I scrap the Mikes jets and go back to the stockers? I didn't have a real reason to change, I did it "just because". AFAIK, they were the same jet sizes, but I didn't write it down so that could be part of the problem I guess.
Looking at three days of heavy rain so this is the perfect time to putter in the garage for a while. Got to put my new clutch and throttle cables from 650 Central on anyway.