Got it outside, took advantage of the no rain day to see if I could get it running.
With all the stuff I've done while waiting for the paint work, I needed to get it all back together. First, I needed to put on the vacuum petcocks I had refurbished to see if they wouldn't leak anymore, and let me just say...Ugh! Super frustrating...one works great...the other, not so much! I used some kits (Mikesxs) and it seemed to fix the right side petcock, but the other weeped like a mountain spring! Crap! So I tore it apart 4 times, knowing it was useless...the valve just wasn't sitting well. I check on here a few times to see if there was something I was missing...and one tip was to polish the seat...which I did...but no go. I pretty much gave up and was getting ready to order a new set of non-vacuum petcocks and be done with it...but then I thought, what if I just use the old valve? And low and behold, it worked. For how long? I don't know...but no leaking fuel meant I could get the tank back on!
I turned on the key, and two kicks later...that beautiful rumble! And then cough/pop/cough/pop...and it died. Ha ha...I had forgotten to put on the vacuum lines, and forgot to set the idle screw...but once adjusted, it came to life and stayed purring.
Then I noticed the tail light went out... but brake light still worked... so found a replacement bulb...and I was off!
With the new rearsets, I needed to adjust those to fit my stance... easy!
One thing I noticed is that I was having a hard time shifting. I could get into first easy enough...but couldn't get back into neutral...I could skip to 2nd, 3rd and so on...and come back down to first, but would still skip neutral...Back when I took off the side cover to replace the sprockets, I'm pretty sure the clutch rod and adjuster wasn't touched, but I must have done something as it wasn't feeling as smooth as I had had it. During the ride I adjusted the cable at the lever...and that seemed to help, but the adjustment screw was WAY out. So tonight I adjusted the screw on the side cover...tightened and then back out 1/4 turn. Have yet to test it, but it feels like it's pulling (or pushing in?) a lot better...we'll see soon enough.
Anyways, short update. so far so good.